Journey with Confidence RV GPS App RV Trip Planner RV LIFE Campground Reviews RV Maintenance Take a Speed Test Free 7 Day Trial ×
 

Go Back   Winnebago Owners Online Community > WINNEBAGO TECH & TOW > General Maintenance and Repair
Click Here to Login
Register FilesRegistry Blogs FAQ Community Calendar Today's Posts Log in

Reply
 
Thread Tools Search this Thread Display Modes
 
Old 12-21-2023, 03:38 PM   #1
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
2019 Navion 24D slide out crooked

Lippert slide out, controller model LCI 366701

Front slide portion is extended about 2 inches, but back slide portion never extended. Attempting to use slide in button does not retract slide.

I've deenergized and reenergized the controller. Unplugged one motor, then the other, swapped plug/cable combinations, and tried to retract. No joy in any combination.

I have not yet performed page 24 "Manual Override Mode - Auto-Program Controllers" to disengage motor and manually retract because there is rain the next day or so and I don't want to have the RV not be sealed. My weather seals that I think I have to pull off to get to the slide motor seem to be glued on.

Any thoughts about what I could/should do before I start pulling off weather seals or bringing this thing to a repair facility?

Manual for my slide: https://lci-support-doc.s3.amazonaws...cd-0004319.pdf
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 11:28 AM   #2
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
Update with more symptoms

Disengaged controller. Took off decorative trim, weather seals, and structural hold down. Disengaged motor. Realigned front and back.

Restored strutural hold down. Reengaged controller.

Now, front and back move, but I'm not sure they move at the same rate. I'll provide update on this later.

Front motor does sound strained.

Lippert 366701 Controller throws Motor 1 fault (1 green, 4 red).

Thoughts?
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 12:19 PM   #3
Winnebago Master
 
Join Date: Nov 2018
Location: Pflugerville/Austin, Tx
Posts: 7,543
Not read the manual on this specific type but there is a process they recommend to help the motors stay together. Since each motor will work slightly different, they often recommend just holding button a few seconds after it looks like the slide is fully out or in as it is designed to have some "slack" and that lets the slower motor and gear catch up.
__________________
Richard
Why no RV year, make and floorplan on MY signature as we suggest for others?
I currently DO NOT have one!
Morich is online now   Reply With Quote
Old 12-22-2023, 05:00 PM   #4
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
I tried that to no avail. Another update coming in now.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 05:22 PM   #5
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
Update with yet more symptoms

Took off inner trim pieces to get to watch the motor to determine the sound.

Jogged out a couple of inches. Noise now gone...but...

Now the front motor (the one that was squealing a bit ago) seems to be faster on the extending cycle than the back motor.

Extended about 1 foot. Front it about an inch further out.

Retracted the same 1 foot. Front is now 1 to 2 inches out when the back is fully retracted.

I'm taking the day now. I now know I can get to and replace either or both motors and the controller. I'd be annoyed, but not $1K annoyed.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 05:32 PM   #6
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
I know I said I was taking the day. I lied.

I just attempted to use emergency jog (one motor at a time) to retract back to even. When I pressed IN, it moved OUT. I unplugged it and plugged it back in to the controller. When I pressed IN, it moved IN.

Why does it INTERMITTENTLY go the opposite direction? I suspect the controller has lost everything. Sometimes it thinks it's at the stops. Sometimes it gets the demand signals backwards.

I'm gonna bite the bullet and get a new controller and try that.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 05:36 PM   #7
Winnebago Master
 
Join Date: Nov 2018
Location: Pflugerville/Austin, Tx
Posts: 7,543
Quote:
Extended about 1 foot. Front it about an inch further out.

Retracted the same 1 foot. Front is now 1 to 2 inches out when the back is fully retracted.


Am I reading this right? When going out the front is faster and getting ahead?
But coming back in the front is slower and left even further out than the other?

I think of these motors as simple direct current motors which run in opposite directions if the polarity of the power is swapped.
If that is all true, one motor is faster going out, then slower coming back in?
Since all the parts of the motor are the same when going out or coming in, I might first look at what it takes to swap the motors and see if it follows the motor?
Next, I might look at swapping out the controller.
Not sure I can see how this is working if all that is what it's doing! Sorry, No really good ideas!
__________________
Richard
Why no RV year, make and floorplan on MY signature as we suggest for others?
I currently DO NOT have one!
Morich is online now   Reply With Quote
Old 12-22-2023, 07:26 PM   #8
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
Yes, you're reading that right. Here's what I think is happening...the controller is intermittently sending signals, sometimes right, sometimes not, sometimes out of good timing, sometimes not, to the motors.

This is resulting in...interesting outputs.

Best case scenario...after I buy and install the new controller, everything clears up.

Worst case scenario...there is a voltage or grounding issue that is making one or both of the motors act crazy.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-22-2023, 09:36 PM   #9
Winnebago Master
 
Ray,IN's Avatar
 
Join Date: Aug 2001
Location: North America somewhere
Posts: 2,115
I'd do the simple, free things first. Completely disconnect (one at a time) each ground connection, clean and re-attach. Do the same for the pos connections. This includes all connection plugs in the wiring. Don't forget battery cable connections. Test again.


That few hours of work isn't worth more than that $1k though, right?
__________________
2000 Winnebago Ultimate Freedom USQ40JD, ISC 8.3 Cummins 350, Spartan MM Chassis. USA 1SG, retired;PPA,Good Sam Life member,FMCA. "We the people are the rightful masters of both the Congress and the Courts - not to overthrow the Constitution but to overthrow men who pervert the Constitution." Abraham Lincoln
Ray,IN is offline   Reply With Quote
Old 12-23-2023, 07:18 AM   #10
Winnebago Master
 
Join Date: Nov 2018
Location: Pflugerville/Austin, Tx
Posts: 7,543
A bit of contact cleaning in any plug in ports on the controller might also be a good idea?
__________________
Richard
Why no RV year, make and floorplan on MY signature as we suggest for others?
I currently DO NOT have one!
Morich is online now   Reply With Quote
Old 12-23-2023, 08:00 AM   #11
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
. I did those things as well as I know how.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-24-2023, 12:28 PM   #12
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
2023-12-24 refresh on all symptoms from initial onset

****First symptoms:

Lippert slide out, controller model LCI 366701

Front slide portion is extended about 2 inches, but back slide portion never extended. Attempting to use slide in button does not retract slide.

I've deenergized and reenergized the controller. Unplugged one motor, then the other, swapped plug/cable combinations, and tried to retract. No joy in any combination.

I have not yet performed page 24 "Manual Override Mode - Auto-Program Controllers" to disengage motor and manually retract because there is rain the next day or so and I don't want to have the RV not be sealed. My weather seals that I think I have to pull off to get to the slide motor seem to be glued on.

****Update following:

Disengaged controller. Took off decorative trim, weather seals, and structural hold down. Disengaged motor. Realigned front and back.

Restored strutural hold down. Reengaged controller.

Now, front and back move, but I'm not sure they move at the same rate. I'll provide update on this later.

Front motor does sound strained.

Lippert 366701 Controller throws Motor 1 fault (1 green, 4 red).

****Update following:

Took off inner trim pieces to get to watch the motor to determine the sound.

Jogged out a couple of inches. Noise now gone...but...

Now the front motor (the one that was squealing a bit ago) seems to be faster on the extending cycle than the back motor.

Extended about 1 foot. Front it about an inch further out.

Retracted the same 1 foot. Front is now 1 to 2 inches out when the back is fully retracted.

****Update following:

I just attempted to use emergency jog (one motor at a time) to retract back to even. When I pressed IN, it moved OUT. I unplugged it and plugged it back in to the controller. When I pressed IN, it moved IN.

Why does it INTERMITTENTLY go the opposite direction? I suspect the controller has lost everything. Sometimes it thinks it's at the stops. Sometimes it gets the demand signals backwards

****Update following:

Tried normal mode again. Front and back seemed to extend and retract at the same rate. Front started about 2 inches early, but kept the same offset.

Disconnected back motor from controller. Back will retract, but not extend so I can't resolve the offset (without manually disconnecting motor).

Swapped to front motor from controller only. Front will extend but only retract to the point of offset, so I still can't resolve the offset (without manually disconnecting motor).

Good news is now the slide is extended far enough that I can access inner and outer trim on front and back.

New controller and motors on the way. I still suspect controller is intermittently losing its mind.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-25-2023, 09:06 AM   #13
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
Update - things working

Did a basic disassemble-reassemble job. I think the reason the front did not fully retract was due to coupler rotated 1 flat off optimal.

Everything else seems normal except more friction noise on both front and back than I remember.

I think this may be solved.

Going for lubrication and complete the reassembly.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-27-2023, 06:59 PM   #14
Willow Rider
 
WillowRider's Avatar
 
Join Date: Aug 2020
Posts: 57
Just to add another angle to the topic, the slide on our 2021 24D started misaligning when a couple teeth broke on the rear rails. Our ESP paid to have the slide rails replaced and all realigned. Problem fixed. Just a thought …
__________________
Willow Rider
2021 View 24D
2020 Sprinter Chassis
WillowRider is offline   Reply With Quote
Old 12-27-2023, 08:10 PM   #15
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
Oh man. I hadn’t thought of a real mechanical failure. I guess I have something to look for if it keeps up.
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Old 12-28-2023, 07:56 AM   #16
Winnebago Camper
 
Join Date: Aug 2023
Posts: 9
My lippert has a similar problem. One of the 3 slides, the rear goes out faster, and 3 inches further than the front. When I shove the front, out by hand, and my wife presses the control, it opens nearly equally. Then I must do the opposite to close, because the rear closes slower. I need the exercise, so I have decided to live with it. I use Tri Flow spray lube, on the flat sprockets.
Rixthe1 is offline   Reply With Quote
Old 12-28-2023, 08:40 AM   #17
Winnebago Camper
 
Join Date: Dec 2022
Location: Palacios, TX
Posts: 19
That’s interesting. My slides don’t respond to pushing pressure as an
__________________
Long Han, 2019 Navion 24D, diesel generator
Mods: after market TPMS; Towed: 2016 Honda HR-V EX manual transmission with simple battery maintainer from 7 pin power
sixthscroll is offline   Reply With Quote
Reply

Tags
slide, slide out


Currently Active Users Viewing This Thread: 1 (0 members and 1 guests)
 

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are Off
Pingbacks are Off
Refbacks are Off


Similar Threads
Thread Thread Starter Forum Replies Last Post
2019 Navion 24D Slide-out Pulled Wires From Conduit HFA Winnebago Class C Motorhomes 3 05-18-2019 07:44 AM
Crooked steering wheel nbounder Running Gear, Axles, Brakes, Wheels and Tires 8 04-11-2013 08:20 PM
Journey slideout canopy is rolling up crooked? asheville General Maintenance and Repair 12 02-26-2008 01:51 PM
living room slide goes out crooked peter griffin General Maintenance and Repair 8 05-31-2007 05:32 PM

» Featured Campgrounds

Reviews provided by

Disclaimer:

This website is not affiliated with or endorsed by Winnebago Industries or any of its affiliates. This is an independent, unofficial site.


All times are GMT -6. The time now is 01:09 PM.


Powered by vBulletin® Version 3.8.8 Beta 1
Copyright ©2000 - 2024, vBulletin Solutions, Inc.